Abstract:The liner cementing under high temperature and high pressure in slim-hole is difficult. Well Long-16 is an important preliminary prospecting well in Chuanbei low and flat fold belt of Jiulongshan structure. The original 2159mm hole was designed to complete in Permian, but as well kick and circulation loss happened frequently, 1778mm casing was put down to cement the upper well section ahead of schedule. In this case, 1492mm bit was used to 598800m, and liner cementing was completed. Before cementing, oil gas showed strongly with drilling fluid density of 234g/cm3 and well temperature of 1396℃.